화학공학소재연구정보센터
SPE Reservoir Engineering, Vol.9, No.3, 217-223, 1994
FIELD-TEST OF COSURFACTANT-ENHANCED ALKALINE FLOODING
A test of cosurfactant-enhanced alkaline flooding, without polymer for mobility control, was conducted in a small reservoir in the White Castle field, Louisiana. Although the flood was unstable, the process recovered at least 38% of the waterflood residual oil in the reservoir as true tertiary oil and exhibited virtually 100% displacement efficiency. Alkali and cosurfactant propagated through the reservoir with acceptable and predictable losses.