Process Safety and Environmental Protection, Vol.88, No.1, 47-52, 2010
Performance of a pilot scale up-flow septic tank for on-site decentralized treatment of residential wastewater
The aim of this research was to study the on-site anaerobic treatment of a medium-strength residential wastewater in a pilot-scale up-flow septic tank (UST). The effects of three different hydraulic retention times (HRTs) of 24, 12 and 6 h on the UST performance were investigated. The UST removed 85, 77, and 86% of biochemical oxygen demand (BODs), chemical oxygen demand (COD) and total suspended solids (TSS), respectively, at steady state operation and with a 24 h HRT. Decreasing the HRT to 12 and then 6 h resulted in deteriorated effluent quality and significantly reduced reactor performance. The sludge showed a high specific methanogenic activity (SMA) of 15.2 mL CH(4) g(-1) VSS d(-1) with raw wastewater substrate. The solids accumulated in the tank by the end of the experiment had a VSS/TSS of 0.57, demonstrating significant stabilization. overall, the LIST is concluded to be a technically and economically promising alternative to conventional septic tanks for the on-site decentralized treatment of residential wastewater, particularly in the rural communities of developing countries. (C) 2009 The Institution of Chemical Engineers. Published by Elsevier B.V All rights reserved.